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MichaelPage - 15:55, Tuesday 16 March 2021 (2398)Get code to link to this report
IRMC Phase shifter jitter noise measurement

Michael and Yuhang

We completed the setup as per 2393. The spectrum of aligment noise from excitation of the IRPS was made and compared to 1904.

 

The measurement was taken using a 500 Ohm PSD placed after the IRMC and homodyne flipping mirror. We measure the dark noise, followed by the jitter noise when transmitting the local oscillator, and then the jitter noise when the phase shifter PZT is excited by random noise from the spectrum analyser, applied via the high voltage driver. In the original measurement of 1904, the PZT was excited using 200 mVpk random noise, where the beam had a horizontal angle of incidence of ~ 45 degrees. Here, the beam has perpendicular incidence, so we only use 200/sqrt(2) ~ 140 mVpk excitement for the yaw measurement, but keep 200 mVpk for the pitch measurement.

For yaw, we seen that the noise floor seems to be the same or perhaps slightly better than 1904, it is hard to tell just from the picture. However, the new measurement reaches the noise floor at approximately 30 Hz, compared to ~ 10 Hz in the old measurement. Also, both measurements have similar values at either end of the measurement frequency window, but the new measurement looks to be a lot higher in the mid frequencies than that of the old measurement. The PD dark noise is consistent in both cases.

For pitch, the measurement is very strange. Unlike yaw in this case and both degrees in 1904, the LO jitter noise does not converge to the PSD dark noise at high frequency. Both the LO jitter and excitation jitter seem to be about 15-20 dB higher than their yaw counterparts.

Afterwards, we measured the transfer function of input excitation (from the spectrum analyser) to measured PSD noise. We see that the pitch transfer function has significantly more coherence from the excitation to the PSD. The yaw coupling at 140 mVpk excitation is also much lower than for pitch excitations.

 

A few other notes:

- The IRMC alignment seems to drift quite a lot. Last week it had to be relocked about 4 or 5 times during the afternoon. It also had dropped to about 1.6 mW transmitted power before starting the measurement described in this elog. I realigned it for the optimal transmission each time (1.8 mW).

- The phase shifter is not quite flat, it has some pitch tilt. As a result, the incoming alignment is not perfectly horizontal, but rather is adjusted so that the outgoing beam maintains a constant height of 76 mm.

- PSD output voltage was zeroed to within 0.5 mV for both X and Y

 

Images attached to this report
2398_20210316064558_irpsexciteyaw2.png 2398_20210316064604_irpsexcitepitch2.png 2398_20210316064609_irpstfyaw2.png 2398_20210316064613_irpstfpitch2.png
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MarcEisenmann - 14:48, Tuesday 16 March 2021 (2400)Get code to link to this report
Comment to large PR/BS drift & air leakage (Click here to view original report: 2397)

Aso-san, Marc

The air leakage of the gate valve was indeed due to a loose screw.

Aso-san tighten it more and no more audible sound nor air coming out.

R&D (FilterCavity)
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YuhangZhao - 14:45, Tuesday 16 March 2021 (2399)Get code to link to this report
Mirror drift again on 20210316 due to earthquake

On Japanese standard time 04:56 JST 16 Mar. 2021, an earthquake happened close to Tokyo area. (attached figure one) 

I checked the oplev signal during this time in the saved data of DGS. PR, input and end mirrors reached the maximum of oplev sensing range. Besides, this oscillation lasted for almost 20 seconds and the exponential decay lasted for almost 40 seconds. (attached figure two)

After the earthquake, all mirrors drifted away from their original position. (attached figure three)

  Yaw_original position Yaw_new position Pitch_original position Pitch_new position
PR 150 320 500 -2000
BS -120 -90 -1200 -1700
Input 3200 3200 500 -2000
End -900 -1700 -1200 3500

According to the above table, we are going to move picomotor to recover mirror position.

Before moving picomotor, I also checked the spectrum of all mirrors pitch/yaw. No touching induced peaks were found. (attached figure four)

Images attached to this report
2399_20210316064615_47.png 2399_20210316064628_27.png 2399_20210316064636_34.png 2399_20210316064641_43.png
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MarcEisenmann - 12:19, Tuesday 16 March 2021 (2397)Get code to link to this report
large PR/BS drift & air leakage

Marc, Yuhang

Yesterday we wanted to check again QPD demodulations pahses before implementing the new driving matrix.

However, the BS pitch seemed to be totally out (180 offset required to get the beam on the end camera).

We had a look on one week data trend of every mirror oplev signal (attached pdf).

This large BS offset has 3 origins as indicated by the red arrows :

  1. An earthquake not too far from Tokyo in March 3d caused a -500 pitch offset of BS (also visible on IN and slightly on END but not so evident effects on PR )
  2. Switching the air conditioning to 'cold mode' cause a 1500 pitch offset of PR. Indeed, PR is located directly under the air conditioning.

  3. Strong rain/storm on March 13th cause a further 500 pitch offset of PR

Therefore we decided to use PR pitch picomotors to move PR back to its previous good position (~300 steps).

But this made the required BS offset -180... This is quite close to coils saturation (it corresponds roughly to 20 000 counts) so we might have to move again BS picomotors...

After the movement of PR picomotor we took the oplev signals (fig 1) where green/brown are references and blue/red yesterday data.

We can see that PR seems fine. However, comparing the low frequency spectrum of BS and PR between reference and yesterday datas, PR low frequency spectrum changed quite more than BS one. It seems that PR is far more sensitive to seismic activities than BS?

We also found out that there is an air leakage on the BS gate valve. It might be due to a loose washer pointed by Yuhang in Fig 2. It might be another after effect of the large earthquake as the air leakage sound was not so easy to hear.

Images attached to this report
2397_20210316041312_20210315oplev.png 2397_20210316041834_20210315airleakage.jpg
Non-image files attached to this report
Comments related to this report
MarcEisenmann - 14:48, Tuesday 16 March 2021 (2400)

Aso-san, Marc

The air leakage of the gate valve was indeed due to a loose screw.

Aso-san tighten it more and no more audible sound nor air coming out.

R&D (FilterCavity)
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MarcEisenmann - 21:13, Friday 12 March 2021 (2396)Get code to link to this report
QPD phase tuning and trial for sensing matrix

Marc, Yuhang

Yesterday we spent some time to tweak a program made by Julia Casanueva for Virgo automatic alignment and adapt it to our case.

Then, we tried to measure the sensing matrix.

However, the green beam was not anymore centered on the QPDs..

We found out that the last steering mirror before the QPDs board was not well fixed. We fixed it back but we could not recover the alignment by acting only on this mirror.

It could mean that another mirror on the green reflection of the FC has been misaligned but we couldn't find which one so we acted on the both galvos to recenter the beam on the QPDs.

We measured the sensing matrix by injecting a 2Hz line on Input and End mirror pitch (300 amplitude) and yaw (200 amplitude) and extracted a driving matrix and phases to get all signal on I quadrature.

 

Today, we saw that the phases are tuned at the level of each segment so we will have to tweak a bit more the program as it gives the optimal phases at the level of pitch and yaw (not individual segment).

Anyway, today we tuned each segment phase 'by hand' to get all signal on I quadrature by either looking at the 11 Hz resonance of pitch or injecting a 2 Hz line. During this measurement the misalignment of the FC affected the accuracy of the measurement so we had to realign it, but also there were moment with large changes of the optimal phases...

The new phases are :

  segment 1 segment 2 segment 3 segment 4
QPD1 125 125 120 127
QPD2 -16 145 -15 -9
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MichaelPage - 11:38, Thursday 11 March 2021 (2395)Get code to link to this report
Phase shifter replacement to reduce jitter noise

We completed the arrangement of the optics described in 2393.

A bit of misalignment from an ND filter in front of the 250mm lens was corrected, and some slight account had to be made for the phase shifter not being perfectly vertical (i.e. introducing pitch misalignment from horizontal incidence). The IRMC mode matching was optimised through alignment and fine tuning of the 75mm and 250mm lens positions, and we recovered the transmission of 1.79 mW of TEM00 from the IRMC (power meter measurement).

We will compare the new result to that of 1904

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MichaelPage - 15:44, Wednesday 10 March 2021 (2393)Get code to link to this report
Phase shifter replacement to reduce jitter noise

Michael and Yuhang

We worked on replacing the phase shifter for the beam going into the IRMC, highlighted in figure 1. Afterwards we will also look at the one going into GRMC. The angle of incidence causes beam jitter noise when the phase shifter acts on the beam. We decided to replace this with a perpendicular incidence setup as per the sketch in figure 2, using a PBS and waveplates.

We have reference for the values of the IRMC (390 µm beam waist, 1.8 mW transmitted power). Using the reference waist and the distances of the holes, the beam should be collimated before the 250 mm lens (fig 3). So there is not much need for complicated rearrangement of the lens positioning. We just have to move the 250 mm forward by however much the path length is from the PBS to the phase shifter and back. Fine tuning of the lenses can be done via the mount. A rough indication of the distances is shown in fig 4.

We took the following items:

PBS: CVI PBS-1064-100

HWP: CVI QWPO-1064-08-2-R10

QWP: CVI QWPO-1064-09-4-AIR-R10

During the aligment we made sure to recheck the beam propagating along the west end of the table to the 250 mm lens, to make sure it aligned with the holes and was consistent with the more recently aligned beam height from the SHG (76 mm).

Using the power meter, the power before the PBS was 4.14 mW. After double passing through QWP and PBS, it was ~ 3.8 mW.

Images attached to this report
2393_20210310074022_20210310layout.png 2393_20210310074031_20210310phaseshiftreplace.png 2393_20210310074037_20210310jammt.png 2393_20210310074044_20210310positioning.png
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MarcEisenmann - 23:19, Tuesday 09 March 2021 (2392)Get code to link to this report
ATC clean room laser setup for OPO assembly

Akutsu-san, Marc, Matteo

In agreement with Akutsu-san we plan to use the ATC clean room to assemble the new OPO.

Fortunately, there is an IR laser installed on one corner that we can use. After the laser source, there are some optics (Faraday Isolator, lenses) so that the beam should be collimated.

The procedure to turn on the laser is the following :

- Connect power supplies

- Turn on the +5V supply (largest black button)

- Press 'stand-by' button on the laser source to get out of the standby mode

There are few components around this laser setup that we can displace for the assembly (scale, forks, pillar) so that with 2 steering mirrors we have enough space to use this laser.

PS :

- We have to bring new clean suits and we can also bring the old ones of this clean room for the next time we clean the clean suits

- we'll need a periscope, beam profiler, mounts, forks, few lenses, safety glasses, etc ...

KAGRA MIR (General)
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MarcEisenmann - 20:39, Tuesday 09 March 2021 (2391)Get code to link to this report
realignment and beams profile measurement

Marc, Matteo

Last Friday I flipped the surface reference sample and tried to further tweak the alignment without much improvement.

Yesterday, we decided to measure the beams profile.

Unfortunately the automated LabView program had some error and we had to do measurement one step at a time...

I installed first the razorblade vertically (2 cm in front of the last hole of the translation stage toward the imaging unit) and scanned both the red and IR beams on the Y/Z axis.

[Note that connecting the DC output of the powermeter went smoothly despite troubles to read the powermeter through the other cable]

Then I turned the razorblade horizontally (54mm above the translation stage) and scanned both the red and IR beams on the X/Z axis.

Actually the razorblade cut the beam not on the razor edge... meaning that we have to take into account the 28mm width of the blade.

I finished to write some MATLAB code to automatically extract all measurement data from yesterday, fit them using a program wrote by Manuel.

But It is still needed to check the screenshots 1 by 1..

KAGRA MIR (General)
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MarcEisenmann - 20:30, Tuesday 09 March 2021 (2390)Get code to link to this report
preparation of KAGRA spare

Marc, Matteo

Yesterday we removed the first contact applied on KAGRA spare, flipped the mirror and applied first contact on the other surface (Fig 1)

Images attached to this report
2390_20210309122945_img20210308103928.jpg
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YuhangZhao - 11:45, Monday 08 March 2021 (2389)Get code to link to this report
Efforts making bench able to be closed

Michael and Yuhang

We replaced the big mirror mount in front of AMC with a compact one. (attached figure 1: the replaced mirror. attached figure 2: the gap between replaced mirror and board)

We have made homodyne DC cable, homodyne power cable, AMC DC PD power cable go through the appropriate hole. (figure 3: extended cable on homodyne power side. figure 4: current cables situation around homodyne)

To close bench, we still need to drill holes on board to let GR inj/ref and IR inj/ref go through (three holes are expected). 

Images attached to this report
2389_20210308034454_wechatimg732.jpeg 2389_20210308034500_wechatimg731.jpeg 2389_20210308041051_wechatimg733.jpeg 2389_20210308041056_wechatimg734.jpeg
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YuhangZhao - 11:33, Monday 08 March 2021 (2388)Get code to link to this report
Signal and noise investigation for CCFC PD (2)

Marc, Michael and Yuhang

We have characterized some signal and noise of CCFC PD in elog2384. However, the pump power was 30mW in that case. According to the simulation and experiment, for the current system, 18mW of pump power would be better. Therefore, we did more test with 18mW pump.

In the attached figure, some signal and noise levels are shown. From this plot, 18mW pump power seems to be not large enough. Indeed, we also tried to close anyway the loop with such small error signal. But we couldn't find a good filter configuration to make the loop closed proporly.

Images attached to this report
2388_20210308033324_figure1.png
KAGRA MIR (General)
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MatteoLeonardi - 10:46, Friday 05 March 2021 (2387)Get code to link to this report
Comment to Preparation of KAGRA spare measurement (Click here to view original report: 2386)

I confirmed the coating of the surface reference sample is on the side with the written part. Therefore the correct orientation is with that side first (i.e. facing the periscope).

The discrepancy between the current and old measurement as well as the slight asymmetry can be caused by not optimal alignment of pump beam.

KAGRA MIR (General)
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MarcEisenmann - 23:40, Thursday 04 March 2021 (2386)Get code to link to this report
Preparation of KAGRA spare measurement

Aritomi, Marc, Matteo

Today we cleaned a bit the computer room and brought the KAGRA spare to the clean room. We putted first contact on the surface facing outside the protection box.

Then, we followed the realignment procedure described on the wiki and installed the surface reference sample to realign the setup with the goal of reproducing the calibration done in elog 1619 : R_surf = AC_surfref/(DC_surfref*P_in*abs_surfref) = 16.9 [1/W]

First, we putted the surface with the sample name facing the laser (PS : mirror center in z is 38 mm). Results are presented in figure 1 and gives (with abs_surfref = 0.22) : AC_surfref = 0.17V, DC_surfref = 3.91V, P_in= 16mW -> R_surf = 12.4 [1/W]

Then, we flipped the reference sample (PS : new center at 33.25 mm) to check if it could explain the discrepancy wrt to elog 1619.

During a scan, there were some troubles with some connections and we got several error messages from LabView... We had to restart the computer to use LabView again but there is still some troubles with the power-meter ( detected but not able to connect to the computer)

The result of this configuration is presented in figure 2 and gives : AC_surfref = 0.31V,  DC_surfref = 4.01V, P_in= 15mW -> R_surf = 23.4 [1/W]

This time the AC measurement is not as symmetrical as expected so we'll further tune the alignment tomorrow.

Images attached to this report
2386_20210304153851_29.png 2386_20210304153857_20.png
Comments related to this report
MatteoLeonardi - 10:46, Friday 05 March 2021 (2387)

I confirmed the coating of the surface reference sample is on the side with the written part. Therefore the correct orientation is with that side first (i.e. facing the periscope).

The discrepancy between the current and old measurement as well as the slight asymmetry can be caused by not optimal alignment of pump beam.

KAGRA MIR (General)
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MarcEisenmann - 23:00, Tuesday 02 March 2021 (2385)Get code to link to this report
Restarting the setup

Marc, Matteo

Today we restarted the mesurement setup.
Laser and chopper restarted smoothly.
However, the translation stages were not recording properly their positions.
We had to change the minimum position limits several time to force the translation stages to their home position.
Then it could be controlled properly from the computer.

We also notice that the readout photodiode is misaligned even without sample.

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YuhangZhao - 18:56, Tuesday 02 March 2021 (2384)Get code to link to this report
Signal and noise investigation for CCFC PD

Michael and Yuhang

Today, we investigated various signal and noise level from CCFC PD. In addition, the servo noise is also added to be compared with signal level.

Attached figure shows their comparison. There are two signals measured in the figure. One comes from picking off signal with beam sampler(~1%), the other comes from BSN11(~3%). The splitting ratio was measured with power meter (offset has been subtracted).

From this measurement, BSN11 would be suitable for the signal pick-off. By using this signal, probably a bandwidth of ~50Hz could be achieved without reinjecting noise. We will try to lock FC with BSN11.

Images attached to this report
2384_20210302105634_figure1.png
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YuhangZhao - 20:39, Friday 26 February 2021 (2383)Get code to link to this report
Comment to Frequency independent squeezing measurement (6.5dB is achieved) (Click here to view original report: 2382)

We made further anti-squeezing and squeezing measurement. This measurement indicates optical losses to be 19.1%, phase noise to be 20.5mrad.

Therefore, we still have 3% optical losses which are not known.

The ideal sqz-asqz for current set-up and improved set-up are shown as well.

Images attached to this comment
2383_20210226123853_spectrum.png 2383_20210226123901_lossphi.png 2383_20210228070347_sqzasqz.png
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YuhangZhao - 22:47, Thursday 25 February 2021 (2382)Get code to link to this report
Frequency independent squeezing measurement (6.5dB is achieved)

Marc, Michael, Yuhang

Recently, homodyne alignment was optimized. Frequency independent squeezing was remeasured. From this measurement, 6.5dB squeezing was measured. Compared with the measurement in elog1837, 1dB more squeezing has been achieved. The main difference between these two measurements is the homodyne alignment.

In this measurement, 37mW pump power was used. Therefore, there should be 15dB original squeezing.

If we assume 20mrad of phase noise, 6.5dB squeezing corresponds to 19% optical losses.

If we assume 30mrad of phase noise, 6.5dB squeezing corresponds to 17% optical losses.

The old measurement was indicating 26% optical losses. Therefore, at least 7% optical losses has been reduced.

The known losses are 1-(1-7e-2)*(1-1e-2)*(1-3e-2)*(1-2e-2)*(1-3e-2)*(1-1e-2) = 16%. 7% OPO intra-cavity losses, 1% dichroic mirror, 3% Faraday isolator, 2% mirror and lens losses, 3% homodyne efficiency/quantum efficiency, 1% classicial noise. Therefore, about 1% to 3% optical losses are not figured out. We will make more characterization tomorrow.

Images attached to this report
2382_20210225144748_squeezing.png
Comments related to this report
YuhangZhao - 20:39, Friday 26 February 2021 (2383)

We made further anti-squeezing and squeezing measurement. This measurement indicates optical losses to be 19.1%, phase noise to be 20.5mrad.

Therefore, we still have 3% optical losses which are not known.

The ideal sqz-asqz for current set-up and improved set-up are shown as well.

R&D (FilterCavity)
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MarcEisenmann - 19:05, Thursday 25 February 2021 (2380)Get code to link to this report
Filter cavity recovery

Marc, Yuhang

Today we got the FC flashes back.

We acted on all picomotors to realign the beam and remove the OpLev offset.

We then took spectra of the OpLev signals and saw that the End Mirror one showed a broadband increase of the noise floor.

This was due to one of the steering mirror screw being almost loose. Therefore we put it to a better situation and compensated it by acting on the steering mirror on the OpLev laser bench.

We also changed the optical density before the End Mirror PSD as it was previously not so well fixed (fig 1 : current situation)

 

The current Oplev spectra are represented in Fig2 with green/brown the references and blue/red the current ones :

  -  PR and BS show the high frequency noise increase that we hope to solve by using the KAGRA QPDs

  - End pitch exhibits a new peak on pitch around 6 Hz

  - BS pitch exhibits a new peak on pitch around 9 Hz

 

Before locking the FC we would like to further tune the OpLev. Indeed, we fixed all their optics but then did not retune the PSD positions nor check the diagonalizations.

These may explain the new peaks on BS and End Mirror as their optics were moved quite a lot

 

PS : the second target is on remote mode and End mirror picomotors have been disconnected

Images attached to this report
2380_20210225105540_20210225emoplev.jpg 2380_20210225105556_20210225oplevnew.png
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RyutaroTakahashi - 17:37, Monday 22 February 2021 (2378)Get code to link to this report
Recovery of BS suspension

[Takahashi, Matteo, Yuhang, Marc, Michael, Aso]

We opened the BS chamber and recovered the suspension.

  1. Opend the BS chamber from the top.
  2. Checked the status of suspension. The gap between the south-west side of IM and the IRM (magnet box) was too small (<0.5mm).
  3. Shifted the suspension point of IRM to south-west. The gap became larger (>1mm).
  4. Measured the TF of suspension. It was consist with the previous one.
  5. Aligned the BS using the IR beam.
  6. Closed the chamber and started evacuation. Opend the GV for the TMP on BS after the evacuation with the big RP.
Images attached to this report
2378_20210222093600_bsim.jpg